Alright Chaps,
Here is what we've tried, in order:
1. Rebuilt Carb, check good on flow bench, no issues noted. Its a MS MA-4SPA 10-3678 2. Primer Isolated, no change 3. Airbox cleaned, filter changed, no issues noted 4. Plugs clean, checked resistance and bomb tested, other than being gummed up, no issues noted 5. Visually inspected engine mount, induction system, everything firewall foreword 6. Aggressively leaned in pattern, problem continued
Fuel system is gravity fed. I've flown it 50 hours since November (when I acquired it), and this is the first time I've had issues with it. I've reached out the previous owner to see if he's had any history with these issues.
Test flew it again today after tackling the plugs, issue seems to be getting worst (or my imagination is getting the better of me) with occasional roughness when leaned too. The intent was to eliminate the plug and mixture theories, and I think I'm satisfied that neither of those were the issue. Back on the ground, the mag checks are dropping off more than before. Everything is pointing towards mags now. It's just strange that both are going at the rate, at the same time....
Moving forward: the magnetos (slicks) are high time and have been untouched since 2003. Beyond overhauling/replacing those, I'm at a loss. Hopefully we'll test flight new mags next weekend. Oshkosh is rapidly approaching...
-Andy
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